03/28/1933 |
Imperial Airways
Armstrong Argosy II |
Dixmude, Belgium |
A fire,
possibly started by a passenger attempting to commit suicide,
caused the plane to crash killing all 15 aboard. This is thought to be
the first act of sabotage on a commercial airliner. |
10/10/1933 |
United Air Lines
Boeing 247 |
Chesterton, Indiana |
The
aircraft was destroyed by an explosive device using nitroglycerin. This
was the first proven case of sabotage in the history of commercial
aviation. |
02/09/1937 |
United Air Lines
DC-3 |
San Francisco, California |
The co-pilot
dropped his microphone which jammed the controls preventing the
pilot from pulling out of the glide. The plane crashed killing all 11
aboard. |
07/28/1945
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U.S. Army
B-25 |
New York City, New York |
A U.S. Army
Air Force B-25 crashed into the 79th floor of the Empire State
Building in fog, killing 3 aboard and 11 on the ground. |
08/02/1947 |
Brit So Am. Airways
Avro Lancastrain |
Andes, Argentina |
Wreckage of the plane was found on January 19, 2000, 53 years after the plane crashed. |
10/24/1947 |
United Air Lines
DC-6 |
Bryce Canyon, Utah |
While
transferring fuel from one tank to another, the crew allowed fuel to
overfill and overflow out the vent. A design flaw allowed the
gasoline to be carried back in the slipstream to the cabin heater
combustion air intake scoop. When the cabin heater came on, an
explosion and fire destroyed the plane killing all 53 aboard. |
10/08/1947 |
American Airlines
DC-4 |
El Paso, Texas |
As a
prank, a captain riding in the jump seat engaged the gust lock in
flight. The command pilot, not knowing the gust lock had been
engaged, rolled the elevator trim tab with no response. When the
jump seat captain disengaged the gust lock, the aircraft went
into into a steep dive, executed part of an outside roll and become
inverted. Neither the command nor jump seat captain had seat belts on
and they accidentally feathered No. 1, 2 and 4 engines when
they hit the controls with their heads. No one realized it at
the time but the feathering reduced power and allowed the
co-pilot, who was strapped in, to pull out of the dive 350 feet
from the ground. |
06/17/1948 |
United Air Lines
DC-6 |
Mount Carmel,
Pennsylvania |
Carbon
dioxide extinguishers were discharged in response to a fire warning in
the cargo hold. The plane's nose was lowered for an emergency
descent and due to a design flaw, carbon dioxide entered the
cockpit and rendered the crew unconscious after which the plane
crashed killing all 43 aboard. |
09/09/1949
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Canadian Pacific
Airlines
DC-3 |
Sault-aux-Cochons, PQ,
Canada |
The
DC-3 disintegrated in flight outside of Quebec killing all 23
aboard.. A dynamite bomb was planted in the forward
baggage compartment by Albert Guay, a jeweler, in a plot to kill
his wife who was a passenger on the plane. Guay, who assembled the bomb,
had his accomplice, Marguerite Pitre air expressed the bomb on
the aircraft. Ms. Pitre's brother, a clockmaker, helped make the
timing mechanism. The insurance policy was for 10,000 dollars. All
three were hanged for their crimes. |
03/03/1953 |
Canadian Pacific
Airlines
de Havilland Comet |
Karachi, Pakistan |
The first crash of a commercial jet airliner in aviation history. |
11/01/1955
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United Airlines
DC-6B |
Longmont, Colorado |
The aircraft
crashed 11 minutes after taking off from Denver on a flight to
Seattle. John Graham placed a dynamite bomb in his
mother's luggage in the No. 4 cargo hold in order to collect
$37,500 in insurance. A delayed flight caused the bomb to detonate
over flat land rather than the mountains as planned. Forty-four
people were killed. Graham never showed any remorse for
his actions and refused to file any appeals. He was executed for
the crime on November 11, 1956. |
02/01/1957 |
Northeast Airlines DC06A |
New York, NY |
Shortly after lifting off
from La Guardia Airport in a snowstorm, the plane rolled sharply to the
left and crashed on Rikers Island. Several inmates from the Rikers
Island Prison made some heroic rescues and were later pardoned. |
12/01/1959 |
Alleghney Airlines
Martin 202 |
Williamport, Pensylvania |
Crashed onto a mountain
after a malfunctioning compass indicated an erroneous heading. Only one
of the 25 passengers survived, found up in a tree, still buckled in
his seat. This was his second plane crash. |
01/06/1960 |
National Airlines
DC-6B |
Wilmington, North Carolina |
A
despondent passenger detonated a dynamite bomb in his lap blowing the
airliner out of the sky and killing 34 people. He was insured for
1 million dollars. |
10/04/1960 |
Eastern Air Lines
Lockheed 188A Electra |
Boston, Massachusetts |
While
taking off, the aircraft hit a flock of Starlings which were ingested
into the engines. Three of the 4 engines lost power which resulted in
loss of control of the aircraft killing 62 out of 72 passengers
aboard. |
12/21/1961 |
British European
Airways
de Havilland Comet |
Ankara, Turkey |
The
plane assumed an extremely steep climbing angle, stalled and crashed
during takeoff. One of three screws on the captain's horizon
indicator worked its way loose and blocked the pointer on the dial
indicating an incorrect pitch. Twenty-seven of 34 aboard were
killed. |
07/15/1962 |
Indian Airlines
C-47A |
Lahore, Pakistan |
A vulture crashed through the cockpit window and killed the copilot. |
11/23/1962 |
United Air Lines
|
Ellicot, Maryland |
The aircraft
struck a flock of Whistling Swans at night, at 6,000 ft. One, estimated
to be 13 pounds, struck the leading edge of the tail stabilizer,
weakening the structure and causing it to detach. The aircraft lost
control and crashed killing all 21 aboard. |
09/04/1963 |
Swissair
Caravelle III |
Durrenasch, Switzerland |
Without
authorization, the pilot taxied half-way down the runway to try and
clear fog. Braking done during the fog clearing overheated the
brakes. Soon after takeoff, the overheated brakes caused a tire
to burst which damaged a fuel line and started a fire. The
plane crashed shortly after killing all 80 people aboard. |
05/07/1964 |
Pacific Air Lines
Fairchild F-27A |
San Ramon, California |
The aircraft
went into a steep dive and crashed while on a flight from Stockton to
San Francisco, CA. The last message which had to be obtained through
laboratory analysis was "Skipper's shot. We've been shot. I was trying
to help." Francisco Gonzales, a passenger, who had told several people
he was going to kill himself, shot both the pilot and co-pilot
causing the plane to crash killing all 44 aboard. |
06/28/1965 |
Pan American AW
B-707-321 |
San Francisco, California |
Just after the
aircraft took off from San Francisco International Airport the No. 4
engine disintegrated tearing off 25 feet of the right wing. An
emergency landing was safely made at Travis Air Force Base. A plane was
dispatched to pick up the passengers at Travis Air Force Base. While
attempting to land, and in plain view of the passengers, the nose gear
collapsed. |
03/05/1966
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British Overseas
Airways
B-707-436 |
Mt. Fuji, Japan |
The aircraft
crashed into Mt. Fuji after encountering severe turbulence when
the pilot decided to give the passengers a view of the mountain. The
aircraft encountered severe clear air turbulence and started to
come apart in the air before crashing killing 124 aboard. |
04/22/1966 |
American Flyers
Airline
Lockheed Electra |
Ardmore, Oklahoma |
The
airliner crashed into foothills while attempting to land killing 83 of
98 aboard. The captain was incapacitated with a heart
attack during the final stages of the approach. The captain, who
suffered from a long standing heart condition and diabetes, managed to
keep his pilot's license by falsifying his medical records. |
06/23/1967 |
Mohawk Airlines
BAC-111-204AF |
Blossburg, Pennsylvania |
The
airplane crashed after an in-flight fire destroyed the pitch control
systems. All 34 people aboard were killed. A
malfunctioning nonreturn valve allowed hot engine bleed air to flow back
through an open air delivery valve, through the APU and into an
acoustic blanket lined section of the fuselage. This caused flexible
hoses with hydraulic fluid to ignite and lead to an uncontrollable fire.
|
11/22/1968 |
Japan Air Lines
DC-8-62 |
San Francisco, California |
The plane
landed in Pacific Ocean, 2.5 mile short of the runway in the
shallow waters of San Francisco Bay. All 107 people aboard were
safely evacuated off the plane. The aircraft was recovered from
the San Francisco Bay 55 hours after the accident, repaired and
eventually flew back home to Japan and was in service for many
decades. |
04/01/1970 |
Aeroflot
Antonov 24 |
Novosibirsk, Russia |
The aircraft crashed killing 61 of 82 aboard after colliding with a balloon. |
07/05/1970
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Air Canada
DC-8-63 |
Toronto, Canada |
While
landing and approximately 60 feet above the runway, the spoilers were
inadvertently deployed by the first officer causing the aircraft
to fall to the runway and lose the No. 4 engine. The crew then
decided to go-around. While circling to land the aircraft
exploded after leaking fuel ignited. All 109 aboard were killed. |
09/08/1970 |
Trans International Airlines
DC-8 |
New York, NY |
A piece of asphalt flew
up and wedged itself in the right stablizer leading to a loss of pitch
control The plane crashed killing all 11 aboard. |
11/24/1971 |
Northwest Airlines
Boeing 727 |
Ariel, Washington |
Not really an "accident" but:
On November 24, 1971, a man calling himself Dan Cooper boarded a
Boeing 727, Northwest Airlines, Flight 305 at Portland Oregon
bound for Seattle Washington. Soon after the plane took off ,
Cooper, seated in seat 18C, stated he had a bomb. He demanded
$200,000 in cash and several parachutes. After the plane landed
at Seattle, the passengers were allowed to leave. Cooper and
four crew members took off with his instructions to fly towards
Mexico. The pilot was instructed to fly no higher that 10,000
feet and below 200 mph. He asked the flight attendant how to
open the tail stairway and ordered her to the front of the plane.
Shortly after, the crew felt a thud and Cooper jumped from the plane
with a 21 lb. package of money tied to his waist. He was never
heard from again. Despite a massive search, no sign of him was
ever found. The FBI calculated he landed somewhere near Ariel,
Washington. Cooper jumped into the darkness at 7 below zero
temperatures with strong winds and freezing rain. He was not
equipped to survive in the wilderness. Cooper, who became
somewhat of a folk-hero in succeeding years, was probably killed in the
jump or succumbed to the elements. The day after the
skyjacking, FBI agents checked out a Portland man with the name
D.B. Cooper but quickly cleared him. The newspapers picked up on it
and incorrectly call the hijacker D.B. Cooper which stuck and was
never corrected. In 1980, a boy playing on the banks of the
Colombia River found 5,800 dollars in 20 dollar bills buried in
the sand which matched the serial number of the money given to
Cooper. Cooper’s lasting contribution to aircraft design is
the "Cooper Vane," a latching device on Boeing 727s that
prevents the tail stairway from being lowered in flight. |
9/06/1971 |
Pan International
BAC-111 |
Hasloh, Germany |
The
aircraft collided with a bridge, shearing off both wings, after a double
engine failure occurred during takeoff. The water-injection
system to cool the engines during takeoff was inadvertently
filled with kerosene instead of water. |
01/26/1972 |
JAT
DC-9-32 |
Hermsdorf, Czechoslovakia |
The plane
crashed after the detonation of a bomb in the forward cargo hold. A
flight attendant, 22 year old Vesna Vulovic, fell 33,330 feet in the
tail section and although she broke both legs and was paralyzed from the
waist down, survived. She was in a coma for 27 days and it took 16
months for her to recover. |
10/13/1972 |
TAMU
Fairchild FH-227D |
Near San Fernando, Chile |
The plane left
Montevideo bound for Santiago, Chile carrying the Old Christians Rugby
Team. The flight crashed into Andes mountains at 12,000 feet. The
aircraft flew into a rotor zone or mountain wave which led to loss of
control of the aircraft. The survivors were not found until
12/22/72 after two passengers hiked to civilization. Survivors
resorted to cannibalism to stay alive. Twenty-nine of 45 aboard
were killed including five passengers who died in an avalanche on
October 30th. The book and movie "Alive" is based on this
accident. |
12/29/1972
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Eastern Air Lines |
Everglades, Florida |
The crew
of the L-1011was preoccupied with a nose gear problem and the
co-pilot was trying to replace the landing gear indicator
light, while on autopilot and in a holding pattern. As the captain got
up to help, he inadvertently pushed on the yoke releasing the
autopilot. With no ground reference and under nighttime conditions,
the aircraft gradually descended until it crashed into Everglades, 18.7
miles west-northwest of Miami. The accident was caused by the
failure of the crew to monitor the flight instruments during the final 4
minutes of flight and to detect a descent soon enough to
prevent impact with the ground. After spare parts from the
crashed L-1011 were used on other planes, apparitions of the
dead captain, Bob Loft and the FE Don Repo, began to be reported
by Eastern Air Line employees on the planes using the spare
parts. The book and movie "Ghost of Flight 401" is based on this
accident. |
11/3/1973 |
National Airlines
DC10-10 |
Albuquerque, New Mexico |
Out of
boredom, the captain and flight engineer decided to experiment
and see what would happen to the autothrottle system if the circuit
breakers which supplied power to the instruments which measured
the rotational speed of each engine's low pressure compressor
were tripped. This led to engine overspeeding and destruction of the
engine. Pieces struck the fuselage, breaking a window, causing rapid
explosive decompression and a passenger was sucked out of the plane.
The plane landed safely. |
09/10/1976
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Intex Adria Av.
British Airways
DC-9 / Trident 3B |
Gaj, Hrvatska, Yugoslavia |
After a
midair collision caused by an ATC error, killed total of 176
people, the entire shift of controllers were arrested. One was found
guilty of criminal negligence and sentenced to 7 years in jail
but release after a little over 2 years. |
11/29/1976 |
Grand Canyon Air
Piper 32-300 |
Grand Canyon, Arizona |
An unrestrained German Shepard interfered with flight controls and caused the plane to crash. |
05/16/1977 |
New York Helicopter
Sikorsky S61 |
New York, NY |
While passengers were
loading aboard the helicopter on top of the Pan Am building, the landing
gear collapsed causing the helicopter to tip on its side. Four
people, waiting to board the craft were killed by the rotating blades.
One of the blades tore loose and struck a window breaking in two.
One-half of the blade then sailed two blocks striking and killing a
pedestrian. |
12/23/1980 |
Saudi Arabian Airlines
Lockheed L-1011 |
Qatar, Qatar |
Two passengers were sucked out of the plane after a tire exploded in the wheel well causing damage to the fuselage. |
02/09/1982 |
Japan Air Lines
DC-8-61 |
Tokyo, Japan |
The aircraft
flew into shallow water after a struggle with a mentally ill
pilot. During the approach, the captain, known to have mental
problems, put the inboard engines into reverse in an attempt to
destroy the aircraft while the co-pilot and flight engineer battled to
restrain him. Twenty-four of 174 aboard were killed. |
05/25/1982 |
VASP
B737-200 |
Braslila, Brazil |
The aircraft
broke in two after a hard landing killing 2 people. The pilot's
misuse of rain repellant, caused an optical illusion leading to
the hard landing. |
06/24/1982 |
British Airways |
Mount Galunggung,
Indonesia |
The aircraft
flew into a plume from a volcanic eruption at 37,000 feet during
the night. While over the Pacific Ocean, all engines
failed and the windshield lost transparency because of pitting from the
volcanic ash. The first engine was restarted at 12,000
feet, followed by the other three and the plane landed safely at
Jakarta. |
07/23/1982 |
Western Helicopter
Bell UH-1 Huey |
Castaic, California |
During the
filming of "Twilight Zone, The Movie," a helicopter crashed,
killing actor Vic Morrow, 57, and two child actors. The helicopter was
hovering low over a make-believe Vietnamese village when an explosive
charge from the special effects hit the tail rotor of the helicopter
sending it crashing to the ground. One child, Rene Chen, was crushed to
death with the right skid. Vic Morrow and the other child, Myca Dinh
Le, were decapitated. Criminal charges against the production company
were eventually dismissed in a much publicized trial. The civil trail
ended in awards of 2 million dollars to the families of each of the
children and $700,000 to the estate of Vic Morrow. |
12/24/1982 |
CAAC
Illyshin IL-18 |
Guangzhou, China |
A passenger's cigarette
caused a fire in the cabin which led to an oxygen tank exploding. The
plane crashed killing 25 of 69 aboard. |
07/23/1983 |
Air Canada
B-767 |
Gimli, Manitoba, Canada |
The aircraft took off from
Ottawa bound for Edmonton with less than half the fuel required to make
the trip. A computer known as the "Fuel Quantity Information System
Processor" was not working properly so the ground crew made manual
calculations for the amount of needed fuel. However, they used
pounds/liter for the specific gravity factor instead of kilograms/liter.
This was first model of aircraft of Air Canada to use kilograms. The
aircraft ran out of fuel at 41,000 feet. With only standby instruments
(magnetic compass, artificial horizon, airspeed indicator and altimeter)
and no slats or flaps, the plane landed safely on a 7,200 ft. runway at
Gimli, a former Air Force base converted into a racing drag strip. The
plane became known as the "Gimli Glider." The TV movie Falling from the
Sky: Flight 174 was made about this incident in 1995. |
10/28/1983 |
Pennsylvania Airlines
Shorts 330-200 |
Middletown, Pennsylvania |
A passenger committed suicide by opening the right rear door and jumping out at 3,500 ft. |
10/11/1984 |
Aeroflot
Tupolev TU-154B |
Omsk, Russia |
The flying control officer
(ATC) fell asleep and did not inform the controllers cleaning vehicles
were on the runway. While attempting to land the aircaft hit the
cleaning vehicles killing 174 of 179 aboard. |
04/16/1985 |
American Airlines
B-727 |
Las Cruces, New Mexico |
While cruising at FL 350 a
loud noise was heard followed by a severe jolt. The No. 3 engine
separated from the aircraft. A damaged O ring allowed leakage from the
forward lavatory waste drain valve. Four gallons of fluid leaked and
froze on the exterior of the plane and then broke away in chunks and
smashed into the engine. The plane landed safely |
08/15/1985 |
Alyemda Airlines
B-707 |
Aden, Yemen |
As the plane reached
FL230, water was spilled on the autopilot panel and the crew had to
disengage the autopilot because the stabilizer trim wheel started to
rotate. Control was lost as the plane pitched up and down. Control was
regained at 1,000 ft. and an emergency landing was carried out. Three of
the 73 passengers aboard were killed. |
12/07/1987 |
Pacific Southwest
Airlines
BAe-146-200a |
San Luis Obispo, Calif. |
A fired USAir
employee, David Burke, after leaving a goodbye message to
friends, shot both pilots. The aircraft went into a steep dive and
crashed killing all 43 people aboard. |
01/08/1989
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British Midland
Airways
B-737-4Y0 |
Leicestershire, England |
While en
route, a fan blade on the No. 1 engine detached and caused a
compressor stall and vibration of the aircraft. The crew throttled back
the No. 2 engine and the vibration stopped and the No. 2 engine was
shut down. While attempting to land, power was lost in the No. 1
engine, the aircraft stalled and crashed a few hundred meters short of
the runway. The plane then slid across the M1 motorway missing many cars
and embedded itself on the west embankment of the motorway. Forty-seven
of the 126 aboard were killed. The crew mistakenly shut down the wrong
engine. |
02/24/1989 |
United Air Lines
B-747-122 |
Honolulu, Hawaii |
After leaving
Honolulu, on a flight from Los Angeles to Sydney, Australia, an
electrical short caused the forward lower lobe cargo door to suddenly
open resulting in explosive decompression and loss of power in
the No. 3 and 4 engines. Nine passengers were sucked out of the
plane and lost at sea but the plane landed safely. |
06/10/1990 |
British Airways
BAC-111 |
Oxfordshire, England |
On a flight
from Birmingham, England to Malaga, Spain, at FL 173, a large section of
windshield fell away from the aircraft. The decompression pulled the
captain out from under his seatbelt. Despite trying to hold onto the
yoke, the captain was sucked out into the opening. A steward in the
cockpit was able to grab hold of his legs. Another steward was able to
strap himself into the vacant seat and aid in holding onto the captain's
legs. The copilot wearing full restraints made an emergency landing at
Southampton. The captain remained half way out of the aircraft for 15
minutes and suffered only frostbite and some fractures. Improper bolts
used to replace the windshield two days earlier resulted in the
accident. |
03/23/1994
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Aeroflot
Airbus A310-304 |
Mezhduretshensk, Russia |
The aircraft
crashed after a captain allowed his child to manipulate the
controls of the plane. The pilot's 11 year old daughter and 16
year old son were taking turns in the pilot's seat. While the boy
was flying, he inadvertently disengaged the autopilot linkage to the
ailerons and put the airliner in a bank of 90 degrees which caused
the nose to drop sharply. The co-pilot pulled back on the yoke to
obtain level flight but the plane stalled. With his seat pulled
all the way back, the co-pilot in the right hand seat could not
properly control the aircraft. After several stalls and rapid pull-ups
the plane went into a spiral descent. In the end, the co-pilot
initiated a 4.8g pull-up and nearly regained a stable flight path
but the aircraft struck the ground in an almost level attitude
killing all 75 aboard. |
05/11/1996 |
ValuJet
DC-9 |
Everglades, Miami, Florida |
An uncontrollable
in-flight fire was caused by activation of one or more oxygen generators
in the forward cargo hold. The generators were outdated, improperly
labeled, lacked safety caps and were prohibited from being transported
on a passenger flight. The plane cashed killing all 110 people aboard. |
10/02/1996 |
Aeroperu
B-757-200 |
Pasamayo, Peru |
The aircraft
crashed into the ocean 28 minutes after taking off from Lima, Peru.
Pieces of duct tape were found covering sensors, placed there by
personnel during aircraft maintenance causing the malfunction of
instruments. The crew was not able to correctly determine their
altitude and airspeed and with no ground reference over water and at
night, crashed into the ocean killing all 70 aboard. A
maintenance worker was tried and convicted of negligent homicide for
failing to remove the adhesive tape and received 2 years in jail. |
11/23/1996 |
Ethiopian Airlines
B-767 |
Off Moroni, Comoros |
The aircraft was hijacked
shortly after taking off from Ethiopia by three drunken escaped
prisoners. They demanded to be flown to Australia, but wouldn't let the
pilot stop to refuel. The plane eventually ran out of fuel and ditched
500 feet offshore killing 127 of 157 aboard. |
04/15/1997 |
Azerbaijan Airlines
Yakovlev 40 |
Gyandzha, Azerbaijan |
A stray bullet from
training soldiers struck the landing plane, hitting an oxygen cylinder. A
fire broke out and control of the plane was lost and it crashed. |
07/23/1999 |
All Nippon Airways
B-747 |
Tokyo, Japan |
Two minutes after taking
off a man carrying a knife forced a flight attendant to take him in the
cockpit of the plane. A fan of computer flight-simulation games, he
stated he just wanted to fly a real plane. After forcing the co-pilot
out of the cockpit he ordered the captain to fly to a U.S. Air Force
base in western Tokyo. When he refused, he stabbed the captain and
seized the controls. After a sudden drop in altitude, the co-pilot and
an off duty crew member entered the cockpit and overpowered the
hijacker. A one point the plane plunged to within 984 feet of the
ground. The plane ultimately landed safely but the captain died of his
injuries. |
05/25/2000 |
Philippine Air Lines
Airbus A-330Near |
Near Manila, Philippines |
A hijacker robbed passengers, jumped out of the plane with a homemade parachute and was killed in the jump. |
08/24/2001 |
Air Transat
Airbus A-330 |
Terceira, Azores |
The Airbus 330, without
engine power, glided for almost 20 minutes, descending from for more
than 30,000 ft. before landing safely at Lajes Airport. Several tires
blew out causing a fire which was quickly extinguished by emergency
crews. The leak was caused by a damaged fuel feed pipe that was caused
by interference from the aft hydraulic pump which was improperly
installed. No one was seriously injured. |
08/27/2006 |
Comair
Canadair CRJ-200ER |
Lexington, Kentucky |
The plane took off from
the wrong runway that was too short. The aircraft ran off the end of the
runway and crashed killing 49 of the 50 aboard. |
08/25/2010 |
Filair |
Bandundu, Congo Democratic Republic |
A passenger brought aboard
a crocodile hidden in a sports bag. The crocodile escaped, causing a
panic among passengers who all rushed to one end of the plane. This
caused an imbalance in the aircraft which led to loss of control and a
crash. |